I used the same system to analyze the Fly Baby accidents
as I use for the overall homebuilt fleet. However,
older accidents (those before 1990 and especially before
1982) had much less data in the reports. The old
reports are pretty cryptic, as well, forsaking a long
narrative about the details of the crash for just a couple
of key words.
Anyway, here's my basic results, compared to what I
compute for the overall homebuilt fleet.
Cause | Fly Baby | Overall Fleet |
Pilot Miscontrol | 29.8% | 39.7% |
Maintenance Error | 10.5% | 4.5% |
Undetermined Loss of Power | 7.0% | 9.6% |
Engine Mechanical | 3.5% | 5.4% |
Fuel System | 3.5% | 3.2% |
Other Mechanical | 22.8% | 4.4% |
Fuel Exhaustion | 3.5% | 3.4% |
Carb Ice | 7.0% | 2.0% |
VFR to IFR | 1.8% | 1.2% |
Manuevering at low alt | 0.0% | 4.3% |
Inadequate Preflight | 1.8% | 1.7% |
Midair Collision | 1.8% | 1.1% |
Loss of Control (Unknown) | 1.8% | 1.4% |
Taxi Accident | 1.8% | 0.5% |
Undetermined | 1.8% | 1.3% |
Other | 1.8% | 4.2% |
So: Why am I not rushing to the airport with an axe and a blowtorch to destroy my Fly Baby? Because there are a few key details.
The first is the circumstances of the failure. About
half (seven) of the fifteen wing-failure cases involved
aerobatics.
But... look at the timing of these accidents. Other
than one in 2007, they stopped in 1982.
NTSB Identification: ATL84FMG03 For details, refer to NTSB microfiche number 24916A
Accident occurred MAR-24-84 at NEW BERN, NC
Aircraft: BOWERS FLY BABY 1A, registration: N4986E
Injuries: 1 Minor.
THE PLT STATED THE ACFT LOST LATERAL CONTROL DURING TAKEOFF. HE REDUCED POWER AND LANDED THE ACFT OFF THE SIDE OF THE RWY WHILE MAINTAINING DIRECTIONAL CONTROL USING THE RUDDER. THE ACFT STALLED AT ABOUT 20 FT AGL AND WAS DAMAGED
DURING THE HARD LANDING. INVESTIGATION REVEALED THAT THE AILERONS WERE NOT OPERATIVE BECAUSE THEY WERE NOT CONNECTED DURING THE PREFLIGHT INSPECTION.
Probable Cause
NTSB Identification: MKC85LA221 For details, refer to NTSB microfiche number 28711A
Accident occurred SEP-21-85 at LEBANON, MO
Aircraft: LON J. MCKNIGHT FLYBABY 1A, registration: N3826
Injuries: 2 Minor.
AFTER WASHING HIS AIRCRAFT THE PLT DPTD THE AIRPORT FOR A LCL FLIGHT. THE FLIGHT LASTED FOR APPROX. 30 MIN. WHEN THE PLT STATED THE END BEGAN RUNNING ROUGH. A PRECAUTIONARY LANDING WAS MADE TO THE AIRPORT. THE ACFT STALLED IMPACTING THE GROUND SHORT OF THE RWY. THE ACFT IMPACTED THE GROUND AT AN APPROXIMATE 40 DEGREE ANGLE. INSP OF THE ACFT ENGINE DID NOT REVEAL ANY MECHANICAL MALFUNCTION.
Probable Cause
NTSB Identification: NYC86LA136 For details, refer to NTSB microfiche number 33126A
Accident occurred MAY-26-86 at MT. PLEASANT, PA
Aircraft: FLY BABY 1-A, registration: N4762
Injuries: 1 Uninjured.
ON SECOND TAKEOFF, AN ABRUPT LOSS OF POWER WAS EXPERIENCED. ON FLARE FOR THE EMERGENCY, OFF AIRPORT LANDING, THE AIRCRAFT LANDED HARD ON RISING TERRAIN, BOUNCED AND CAME TO REST INVERTED.
Probable Cause
NTSB Identification: NYC86FGM06 For details, refer to NTSB microfiche number 31496A
Accident occurred JUL-27-86 at FRANKLIN CENTER, PA
Aircraft: KENNETH PATSCH FLY BABY II, registration: N14OP
Injuries: 1 Fatal, 1 Serious.
THE PLT REPORTED THAT THE ACFT BANKED EXCESSIVELY DURING THE LEFT TURN FROM BASE TO FINAL. OPPOSITE CONTROL INPUT WAS APPLIED, HOWEVER, THE PLT REPORTED THE "STICK SEEMED TO HAVE NO RIGHT MOVEMENT." FULL POWER WAS APPLIED BUT THE BANK STEEPENED SO POWER WAS REMOVED. CONTROL INPUT WAS ATTEMPTED AGAIN AND THIS TIME THE ACFT YAWED 80 DEGREES RIGHT AND THE LEFT WING LIFTED 45 DEGREES. THE ACFT THEN CONTINUED IN THE DESCENT TO GROUND IMPACT. THE PLT SUGGESTED THAT DUE TO REDUCED SPACE IN THE FRONT COCKPIT, THE FRONT SEAT PASSENGER MAY HAVE RESTRICTED THE CONTROL MOVEMENT. FLIGHT CONTROL CONTINUITY COULD NOT BE DETERMINED DUE TO THE EXTENT OF IMPACT DAMAGE.
Probable Cause
NTSB Identification: LAX87DVM02 For details, refer to NTSB microfiche number 34818A
Accident occurred MAR-31-87 at SAN LUIS OBISPO, CA
Aircraft: BOWERS FLYBABY 1A, registration: N792JB
Injuries: 1 Serious.
DURING A PLEASURE FLT IN AN EXPERIMENTAL ACFT, DURING THE TAKEOFF ROLL, THE ENG SPUTTERED, HOWEVER, THE PLT CONTINUED THE FLT. AFTER TAKEOFF AT APRX 30 FT THE ENG SPUTTERED AGAIN. THE PLT MADE A SHARP 45 DEG TURN WHICH PUT HIM ON DOWNWIND, HOWEVER, THE ACFT WAS KEPT IN A NOSE HIGH ATTITUDE. AT APRX 300 FT THE ENG SPUTTERED AGAIN THEN QUIT. THE LEFT WING DROPPED AND THE ACFT COMPLETED ONE TURN AND IMPACTED THE TERRAIN IN A 70 DEG NOSE DOWN ATTITUDE. THERE WERE NO MECHANICAL FAILURES OR MALFUNCTIONS REPORTED.
Probable Cause
NTSB Identification: MKC89DCG01 For details, refer to NTSB microfiche number 39524A
Accident occurred MAY-07-89 at WEST PLAINS, MO
Aircraft: GRIGG/BOWERS FLYBABY, registration: N1305
Injuries: 1 Serious.
THE PLT HAD FLOWN ANOTHER ACFT FROM DIKE, IA TO JONESBORO, AR & HAD TRADED IT FOR N1305, WHICH HE WAS FLYING BACK TO DIKE. HE HAD PLANNED AN INTERMEDIATE STOP AT WEST PLAINS, MO. IN THE VICINITY OF WEST PLAINS, WITNESSES HEARD A POPPING SOUND FROM THE ENG. THE PLT LANDED IN A FLD OF KNEE HIGH GRASS NEAR WEST PLAINS. AFTER REPAIRING A REPORTED PROBLEM WITH A SCREW ON THE CARBURETOR, THE PLT ELECTED TO FLY THE ACFT OUT OF THE FIELD. HE INITIATED A TAKEOFF TO THE EAST ON SLIGHTLY RISING TERRAIN WITH A SLIGHT TAIL WIND. AFTER LIFT-OFF, THE ACFT GAINED LITTLE ALTITUDE BFR RCHG POWER LINES & ENTERED A SHARP TURN. IT THEN PITCHED DOWN & CRASHED. WITNESSES REPORTED THE WIND WAS GENTLE FM THE WEST, BUT MOVEMENT OF TREETOPS INDCD A STRONGER WIND ALOFT.
Probable Cause
NTSB Identification: ATL90DMG01 For details, refer to NTSB microfiche number 41765A
Accident occurred JAN-07-90 at TROY, NC
Aircraft: WALDRON FLYBABY, registration: N91089
Injuries: 1 Fatal.
A NON-RATED PERSON (WITH NO FAA MEDICAL OR PLT CERTIFICATE) ELECTED TO FLY THE HOME-BUILT ACFT. REPORTEDLY, THE ENG BEGAN TO "MISFIRE" WHEN THE ACFT WAS OVER THE ARPT AT ABOUT 1000' AGL. THE PLT ATTEMPTED TO LAND; HOWEVER, THE ACFT SUBSEQUENTLY CRASHED IN A STEEP DSCNT NEAR THE 1600' RWY. NO PREIMPACT PART FAILURE OF THE ACFT WAS FOUND. THE TEMP & DEW POINT WERE 44 & 36 DEG, RESPECTIVELY. ACCORDING TO CARB ICING CHARTS, CONDITIONS WOULD HAVE BEEN CONDUCIVE TO SERIOUS CARB ICING. NO RECORD WAS FOUND THAT THE PLT HAD RCVD PLT TRAINING, THOUGH HE HAD REPORTEDLY FLOWN ULTRALIGHT CRAFT. TOXICOLOGY CHECKS SHOWED HE HAD A (BLOOD)-ALCOHOL LVL OF 0.07O%, & A URINE-ALCOHOL LVL OF 0.145% (145 MG/DL).
Probable Cause
NTSB Identification: MKC90LA116 For details, refer to NTSB microfiche number 42516A
Accident occurred MAY-29-90 at BEMIDJI, MN
Aircraft: ROLLINS-BOWERS FLY BABY 1A, registration: N3204
Injuries: 1 Fatal.
SHORTLY AFTER TAKEOFF, THE HOMEBUILT ACFT, CRASHED INTO TREES. THERE WERE NO WITNESSES TO THE ACCIDENT. POST ACCIDENT INVESTIGATION REVEALED THE ABSENCE OF THE RIGHT WING RETAINING PINS. THE WRECKAGE PATTERN INDICATED THAT THE RIGHT WING HAD SEPARATED IN FLIGHT, WHICH RESULTED IN AN UNCONTROLLED DESCENT. NO MECHANICAL MALFUNCTIONS OR FUEL SUPPLY SHORTAGE WAS FOUND.
Probable Cause
NTSB Identification: CHI90DEM09 For details, refer to NTSB microfiche number 45463A
Accident occurred SEP-13-90 at CHEBOYGAN, MI
Aircraft: COMBEN BOWERS FLYBABY IA, registration: N1175B
Injuries: 1 Fatal.
THE HOMEBUILT AIRPLANE COLLIDED WITH THE TERRAIN IN A WOODED AREA. THE WRECKAGE HAD BEEN REMOVED AND TRANSPORTED TO AN UNKNOWN LOCATION. PHOTOGRAPHS INDICATE THAT THE AIRPLANE IMPACTED THE GROUND IN A STEEP NOSE-DOWN ATTITUDE. THE PILOT'S LAST FLIGHT PHYSICAL WAS MORE THAN 11 YEARS AGO. NO AUTOPSY.
Probable Cause
NTSB Identification: CHI91DEP09 For details, refer to NTSB microfiche number 44696A
Accident occurred JUN-16-91 at STOUGHTON, WI
Aircraft: BOWERS FLYBABY 1A, registration: N8084D
Injuries: 1 Fatal.
WHILE PERFORMING AN AEROBATIC MANEUVER THE RIGHT WING FAILED AND DEPARTED THE AIRPLANE. THE AIRPLANE THEN DESCENDED INTO THE TERRAIN. SUBSEQUENT EXAMINATION REVEALED WOOD ROT AT THE FUSELAGE CARRY THRU SPAR ATTACHMENT WHERE THE FAILURE OCCURRED. EXAMINATION REVEALED SIMILAR ROT ON THE LEFT SIDE. THERE WERE NO DRAIN HOLES IN THE AREA OF THE SPAR ATTCHMENT WHERE MOISTURE COULD ACCUMULATE. IT WAS FURTHER DETERMINED THAT THE AREA WHERE THE DETERIORATION OCCURRED WAS NOT VISIBLE DURING NORMAL INSPECTION.
Probable Cause
NTSB Identification: CHI93DTG01 For details, refer to NTSB microfiche number 48104A
Accident occurred OCT-22-92 at BUFFALO, ND
Aircraft: KING BOWERS-FLYBABY, registration: N199
Injuries: 1 Uninjured.
THE PILOT EXPERIENCED A PARTIAL LOSS OF ENGINE POWER AFTER TAKEOFF AND MADE A FORCED LANDING IN A PLOWED FIELD ONE-HALF MILE FROM AIRSTRIP. THE INVESTIGATION REVEALED THAT THE THROTTLE CABLE WAS DISCONNECTED FROM THE THROTTLE BODY OF THE CARBURETOR. THE PILOT/OWNER HAD REMOVED AND REINSTALLED THE CARBURETOR TWO HOURS BEFORE THE FLIGHT.
Probable Cause
NTSB Identification: BFO93LA076 For details, refer to NTSB microfiche number 50369A
Accident occurred MAY-09-93 at PEAPACK, NJ
Aircraft: HOCKENBURY BOWERS FLY BABY, registration: N80PH
Injuries: 1 Minor.
WHILE AT CRUISE, THE AIRPLANE'S ENGINE LOST PARTIAL POWER. THE PILOT REPORTED THAT HE APPLIED CARBURETOR HEAT AND CHECKED THE OIL TEMPERATURE AND PRESSURE. THE ENGINE DID NOT REGAIN POWER. THE PILOT ATTEMPTED TO MAKE A FORCED LANDING IN A YARD BELOW THE AIRPLANE'S FLIGHT PATH BUT DURING THE APPROACH TO LANDING, THE AIRPLANE COLLIDED WITH TREES. THE AIRPLANE FELL TO THE GROUND AND CAME TO REST INVERTED. POST ACCIDENT EXAMINATION OF THE AIRPLANE DID NOT REVEAL ANY AIRFRAME ANOMALIES. THE ENGINE WAS DISMANTLED AND EXAMINED. EXAMINATION OF THE CARBURETOR REVEALED THAT THE THROTTLE VALVE ACTUATING ARM, WHICH WAS FASTENED TO THE THROTTLE SHAFT, WAS LOOSE AND THEREFORE WOULD NOT OPEN THE THROTTLE VALVE FULLY.
Probable Cause
NTSB Identification: BFO93LA122. The docket is stored in the (offline) NTSB Imaging System.
Accident occurred JUL-12-93 at CONNEAUT, OH
Aircraft: SCHULTZ/BOWERS FLY BABY 1A, registration: N4295X
Injuries: 1 Serious.
WHILE IN CRUISE, THE AIRPLANE'S ENGINE LOST PARTIAL POWER. THE PILOT STATED HE WAS OVER A FIELD AND DECIDED TO CIRCLE AND LAND IN THE FIELD. THE PILOT STATED THAT DURING THE SECOND TIME HE WENT AROUND THE FIELD, DOWNWIND, THE AIRPLANE'S ENGINE LOST TOTAL POWER. THE AIRPLANE IMPACTED A BERM ON THE SIDE OF A ROAD JUST SHORT OF THE FIELD. WITNESSES TO THE ACCIDENT STATED THAT PRIOR TO THE AIRPLANE IMPACTING THE BERM, THE ENGINE WAS "MISSING." POST ACCIDENT EXAMINATION OF THE AIRFRAME DID NOT REVEAL ANY ANOMALIES. THE COCKPIT MAGNETO SWITCH WAS SELECTED TO THE LEFT MAGNETO. THE ENGINE WAS INSPECTED AND THE LEFT MAGNETO HIGH TENSION LEAD WAS FOUND CORRODED WITH GEAR GREASE CAUSING INTERMITTENT ARCING. SPARK PLUGS ON THE NUMBER 2 AND 3 CYLINDERS WERE FOUND TO BE SOOTY AND THE SPARK PLUGS ON THE NUMBER 1 AND 4 CYLINDERS APPEARED "NOT TO BE FIRING." THE PILOT STATED THAT HE DID NOT LEAVE THE MAGNETO SWITCHED TO THE "LEFT" POSITION AND THAT IT MUST HAVE BEEN MOVED DURING THE IMPACT SEQUENCE.
Probable Cause
Accident occurred Saturday, April 02, 1994 at BISBEE, AZ
Aircraft:CURRY FLY-BABY, registration: N183RC
Injuries: 1 Serious.
On April 2, 1994, at 1000 mountain standard time, a homebulit experimental Curry Fly-Baby, N183RC, collided with rough terrain during an attempted forced landing on a road near Bisbee, Arizona. The forced landing was precipitated by a loss of engine power during the takeoff initial climb. The aircraft was owned and operated by the pilot. Visual meteorological conditions prevailed at the time and no flight plan was filed for the operation. The aircraft was destroyed in the collision sequence. The certificated private pilot, the sole occupant, sustained serious injuries. The flight was originating at the time of the accident as a local area personal flight.
According to the pilot, the aircraft was in the initial climb after takeoff when the engine suddenly quit. The pilot reported that he did not have sufficient altitude or vehicle energy to return to the airport and attempted to land on a nearby road. The aircraft landed short and collided with rough terrain.
In his written report, the pilot said he suspects a fuel blockage at the tank outlet as the cause for the engine power loss.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows.
NTSB Identification: LAX96LA146. The docket is stored in the (offline) NTSB Imaging System.
Accident occurred MAR-28-96 at CASTIAC, CA
Aircraft: LUCKETT FLYBABY 1A, registration: N71658
Injuries: 1 Serious.
The accident site was in a pass at the southern end of a mountain valley. A major interstate highway traversed the mountains through this valley. The pass at the southern end of the valley was characterized by rapidly rising and narrowing terrain. U.S. Forest Service workers near the site reported that the pass and the surrounding terrain was obscured by clouds which went to the ground. The aircraft collided with the side of a mountain about 300 feet above the elevation of the highway. An FAA inspector went to the accident site, interviewed witnesses, and examined the aircraft. He reported that the aircraft was traveling southbound over the highway as it approached the pass. The aircraft collided with the terrain as the pilot attempted to turn around in the narrow pass. Control system continuity could not be established throughout the aircraft due to extensive airframe crush deformation. Fuel was present in the tank and no discrepancies were found in the engine.
Probable Cause
NTSB Identification: CHI98LA233. The docket is stored in the (offline) NTSB Imaging System.
Accident occurred JUL-02-98 at BLISSFIELD, MI
Aircraft: Wicks FLY BABY, registration: N40349
Injuries: 1 Minor.
On July 2, 1998, at 0800 eastern daylight time, a Wicks Fly Baby, N40349, piloted by a commercial pilot, received substantial damage when it impacted the terrain, during a forced landing after a loss of engine power during takeoff from runway 27 (2,585' X 100') at the Betz Airport, Blissfield, Michigan. Visual meteorological conditions prevailed at the time of the accident. The personal 14 CFR Part 91 local flight was not operating on a flight plan. The pilot reported minor injuries. The flight was originating at the time of the accident.
During the initial climb the engine suffered a loss of power. Post accident inspection of the airplane failed to reveal any smell of fuel on or around the wreckage. There was no fuel spill on the ground. Only unusable fuel was found in the tank. No other mechanical anomalies were found during the post accident examination.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows.
Accident occurred Saturday, May 22, 1999 at MOUNT OLIVE, NC
Aircraft:Murray R. Gardner FLY BABY, registration: N96MG
Injuries: 1 Minor.
The pilot recalled that as the airplane descended through 1700 feet, the left wing assembly came up over the cockpit and separated from the airframe. The pilot reported that he always flew this airplane wearing a parachute, and as the airplane entered a spin he was ejected from the cockpit. After clearing the airframe, the pilot pulled the ripcord to deploy the parachute; a full parachute canopy was achieved 300 feet above the ground. During the examination of the airframe the left wing flying wire attachment plate was located and was discovered to have failed. The attachment plate fracture faces were examined with an optical microscope and were found to contain banding, typical of fatigue cracking, on both sides of the attachment hole. The fatigue cracking propagated nearly through the thickness of the plate. Elevated oxygen peaks, indicative of corrosion deposits, were also discovered.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows.
(Further details and analysis of this accident)A fatigue failure of the flywire bracket that resulted in the inflight separation of the left wing.
Accident occurred Saturday, May 13, 2000 at KEYMAR, MD
Aircraft:Hing FLY BABY 1A, registration: N2685
Injuries: 1 Fatal.
According to witnesses, the homebuilt Fly Baby was cruising about 1,500 feet above the ground, in a climb or nose high attitude. The witnesses reported hearing a popping sound, after which the right wing folded up next to the fuselage. The airplane descended, and struck the ground. Examination revealed the two flying wires on the underside of the forward right wing spar were separated from the wing. One wire had failed at its loop through the eye of the turnbuckle, and the other wire separated at a failed turnbuckle. Metallurgical examination found evidence of overload on both failures. According to the designer of the airplane, the airplane had been static load tested to 6gs with no failure. In addition, each pair of flying wires must have similar or matched tension. If one wire was loose, a momentary flight load could exceed the load capability of one wire, which would cause it to fail, followed by the failure of the second wire as it tried to assume the load. The pre-accident tension on the failed flying wires could not be determined.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows.
(Further details and analysis of this
accident)
On November 1, 2000, about 1520 eastern standard time, a Horne Bowers Flybaby, N4041A, registered to a private individual, operating as a Title 14 CFR Part 91 personal flight, crashed in the vicinity of Greer, South Carolina. Visual meteorological conditions prevailed, and no flight plan was filed. The experimental, amateur-built airplane received substantial damage, and the private-rated pilot, the sole occupant, was not injured. The flight originated from the same airstrip about 20 minutes before the accident.
According to the pilot, his landing resulted in an extended flare that touched down at about the mid-length point of the 1,800-foot runway and despite heavy braking on the grassy, down-sloped surface, ran off the runway end and into a fence.
According to an eyewitness to the accident, the flight's first approach resulted in a go-around due to being too high. The second approach was too fast, resulting in a touchdown beyond the mid-length of the runway. The aircraft continued beyond the runway end, collided with a perimeter fence, and nosed over into a drainage ditch.
According to an FAA inspector, the accident occurred in the Lake Cunningham area of Greer, South Carolina, at a private airstrip named Flying Few Airfield. Examination of the aircraft revealed a broken wooden propeller, leading edge damage to the wings, and buckling of the fuselage behind the cockpit. The pilot stated to him that he may not have closed the throttle all the way on landing.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
A runway overrun as a result of the pilot's failure to maintain
proper
approach speed and landing touch down point.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot's failure to return the carburetor heat to the OFF
(cold)
position prior to applying full power following a touch and go
landing,
which resulted in poor climb performance and the subsequent impact
with
a fence and collision with the ground. A contributing factor was
the
fence.
The airplane was observed by a witness flying over a tree line. The nose of the airplane was observed to pitch up to about a 70-degree nose high attitude. The left wing dropped down and the nose pitched down as if the airplane was in a stall and collided with the ground. Examination of the airframe, flight controls and engine assembly revealed no anomalies. The left wing was compressed aft and received accordion crushing from the wing root extending outboard to the wing tip. The Fly Baby 1A Ultra light plans revealed that the stall speed for the Bowers Fly Baby 1A airplane is 45 mph.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain airspeed while maneuvering resulting in a stall.While attempting to return to the airport following a loss of engine power, the airplane contacted rough terrain during a forced landing in an open field about 3,000 feet short of the runway. A wing and the main landing gear were separated from the airplane after touchdown. Following the loss of power, the pilot activated the carburetor heat to no avail. He turned back to the airport and when he knew he wasn't going to make the runway, he made the forced landing. A plot of the temperature and dew point on a carburetor icing chart revealed that the possibility existed for icing conditions at glide and cruise power settings. The pilot stated that there were no mechanical problems with the airplane, and that he should have checked more frequently for carburetor ice during the flight.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
a loss of engine power due to the pilot's failure to use carburetor heat during conditions that were conducive to carburetor icing.The pilot departed the airport for a local personal flight in the amateur built experimental-category airplane. About 25 minutes after takeoff, the airplane was observed flying in an easterly direction at an undetermined altitude. The witness reported hearing the engine slow down and then speed up. Seconds later, the witness heard "what sounded like an explosion" followed by the airplane falling to the ground in multiple pieces. The witness was located approximately 1 mile from where the wreckage came to rest. Post accident examination of the wreckage revealed that the right wing's forward and aft solid flying wires, turnbuckles and respective wire anchor attachment brackets remained intact, however the attachment brackets were separated from the forward and aft spar assemblies. The four through bolts (AN3 3/16-inch-diameter) associated with the forward brackets were fractured along the bolt shank near the bolt head. The bolts were necked down and were bent near the fracture points; the fracture surfaces were angular. Only two of the four through bolts associated with the aft bracket were recovered and similar findings were noted; the bolts were necked down and the fracture surfaces were angular. The builder's instruction manual for the airplane recommends AN3 (3/16-inch-diameter) anchor attach bracket bolts for standard operations and AN4 (1/4-inch-diameter) anchor attach bracket bolts if aerobatics are intended to be performed in the airplane. The specified anchor attachment bracket bolts (both AN3 and AN4) range in length from 5-1/2-inches to 6-3/4-inches. A personal friend of the pilot reported that about 2 weeks before the accident, the pilot completed a flight in the accident airplane. Upon returning from the flight, the pilot stated that he had completed a "slow roll." The pilot stated the airplane performed well during the flight.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot exceeding the design stress limits of the aircraft while maneuvering in intentional aerobatics.The pilot reported that he decided to return to the destination airport after flying for about an hour. After completing a 180-degree turn, the airplane began losing altitude. The pilot reported that the throttle was full-in, and the airplane was maintaining sufficient airspeed; however, the reason for the altitude loss could not be ascertained. The pilot said he then elected to make a precautionary landing in an open field. While on final, the landing gear wheels struck a barbed wire fence, which pulled the wheels up, and the airplane immediately nosed over after touchdown. The pilot reported no mechanical problems that would have precluded normal operation.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The
private pilot was flying cross country in his single-engine
homebuilt
airplane when it collided with wooded and mountainous terrain in
day
visual meteorological conditions for undetermined reasons. The
airplane
was missing for five days before it was located by units of the
Civil
Air Patrol at an elevation of 2,950 feet mean sea level. A Federal
Aviation Administration (FAA) inspector performed an on-scene
examination on the day the airplane wreckage was located.
According to
the inspector, the airplane, which was constructed from wood and
fabric
frame, came to rest at the base of several large pine trees and
did not
burn. The initial impact point appeared to be the tops of the
trees
located directly above the main wreckage, which included the
engine,
fuselage, both wings, and tail section. All flight control
surfaces
remained attached to the airframe. The two-bladed wooden propeller
was
damaged; however, it remained attached to the engine. Engine
continuity
was established via manual rotation of the propeller. The single
fuel
tank was breached from impact forces, and the fuel cap was found
secured to the tank. No anomalies were found with the airframe or
engine that could have prevented normal operation. The pilot held
a
private pilot certificate for airplane single-engine land and also
held
an inspection certificate for experimental aircraft. His last FAA
third
class medical certificate was issued on August 1, 2003. At that
time,
the pilot reported having accumulated a total of 452 flight hours.
The
pilot's logbook and the airplane's maintenance records were not
located
during the course of the investigation.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The airplane's collision with wooded and mountainous terrain for undetermined reasons.
The private pilot conducted a run-up of the experimental airplane's 65-horsepower engine prior to departure, since it had not been flown in the past 90 days. The engine produced full power and the pilot departed the private airstrip. Shortly after takeoff, the engine started to gradually lose power and the airplane was unable to maintain a normal climb rate. The pilot returned to the airport, but had to execute a go-around due to another airplane being on the runway. When he applied full power, black smoke was observed "belching" from the exhaust and the engine power continued to decline. The pilot made a forced landing to a field adjacent to the airstrip and subsequently the airplane sustained structural damage. The pilot reported that there was no air filter installed on the engine and he thought that a nest of mud-dauber wasps had built a nest in the air intake, vibrated loose, and was ingested into the carburetor intake.
The National Transportation Safety Board determines the probable cause(s) of this accident to be:
A partial loss of engine power due to an obstruction of the air intake, as reported by the pilot. Contributing to the accident was the pilot's insufficient preflight inspection.
The airplane veered off the left side of the runway during takeoff and struck an elevated runway light located 600 feet from the end of the runway. The airplane traveled over a shallow grass slope, impacted the hangar door nose first, and embedded itself into the hangar. Both wings separated from the fuselage. The pilot, who was seriously injured, could not recall the events of the accident. A postaccident examination of the airframe revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.
The National Transportation Safety Board determines the probable cause(s) of this accident to be:
The pilot did not maintain directional control of the airplane during the takeoff roll.
Location: |
Mariposa, CA |
Accident Number: |
WPR14FA165 |
Date & Time: |
04/11/2014, 1007 PDT |
Registration: |
N6054Q |
Aircraft: |
WILLIAMS MYRON G BOWERS FLY BABY 1A |
Aircraft Damage: |
Substantial |
Defining Event: |
Loss of engine power (partial) |
Injuries: |
1 Fatal |
Flight Conducted Under: |
Part 91: General Aviation - Personal |
The plans-built
single-seat airplane
had been constructed about 8 years before the accident by
another individual, who had flown it about 30 hours before it
was purchased by the current owner/pilot. In the year since the
purchase, due to the low build-quality of the airplane, the
pilot had made several modifications and repairs to the
airplane. The accident flight was the pilot’s fifth flight in
the airplane. Review of the pilot’s flight logbook indicated
that his most recent flight review occurred about 7 years before
the accident and that he had flown only 15 hours in the 2 years
before the accident.
A witness reported that shortly
after takeoff, when the airplane was about 3 miles from the
airport, the engine began making a sound as if power was
intermittently being interrupted. The nose of the airplane began
to pitch up aggressively as it flew out of view. The wreckage
location, wreckage distribution, and impact signatures indicated
that the airplane struck the ground in a steep nose-low
attitude, consistent with an aerodynamic stall event.
Postaccident examination of the
carburetor revealed multiple maintenance-related discrepancies,
any one of which could have resulted in the loss of engine
power. Additionally, before the accident, the pilot reported to
a friend that the airspeed indicator was not reliable and that
the airplane exhibited roll control anomalies. Both of these
conditions would have hindered the pilot’s ability to safely
operate the airplane.
The National Transportation Safety Board
determines the probable cause(s) of this accident to be:
The partial loss of engine power due to an
improperly maintained carburetor and the pilot's subsequent
failure to maintain aircraft control.
Location: |
Guthrie, OK |
Accident Number: |
GAA16CA180 |
Date & Time: |
04/02/2016, 2005 CDT |
Registration: |
N359RJ |
Aircraft: |
LAMB-ROBIN BOWERS FLY BABY |
Aircraft Damage: |
Substantial |
Defining Event: |
Aerodynamic stall/spin |
Injuries: |
1 Minor |
Flight Conducted Under: |
Part 91: General Aviation - Personal |
The pilot reported that during the initial climb, the airplane aerodynamically stalled. He reported that he was unable to recover the airplane due to the low altitude and the airplane impacted a field off the departure end of the runway. The airplane sustained substantial damage to the fuselage, right wing, and right elevator.
The pilot verified that there were no preimpact mechanical failures or malfunctions with the airframe or engine that would have precluded normal operation.
As a safety recommendation, the pilot reported that using full power on takeoff would have prevented the accident.
The Federal Aviation Administration has published the Airplane Flying Handbook FAA-H-8083-3A (2004). This handbook discusses stalls and states in part:
The key to stall awareness is the pilot's ability to visualize the wing's angle of attack in any particular circumstance, and thereby be able to estimate his/her margin of safety above stall. This is a learned skill that must be acquired early in flight training and carried through the pilot's entire flying career. The pilot must understand and appreciate factors such as airspeed, pitch attitude, load factor, relative wind, power setting, and aircraft configuration in order to develop a reasonably accurate mental picture of the wing's angle of attack at any particular time. It is essential to flight safety that a pilot takes into consideration this visualization of the wing's angle of attack prior to entering any flight maneuver.
Stall accidents usually result from an inadvertent stall at a low altitude in which a recovery was not accomplished prior to contact with the surface.
The National Transportation Safety Board
determines the probable cause(s) of this accident to be:
The pilot's exceedance of the airplane's critical angle of
attack during the initial climb, which resulted in an
aerodynamic stall and a collision with terrain.
Location: |
Milton, FL |
Accident Number: |
ERA19FA020 |
Date & Time: |
10/19/2018, 1130 CDT |
Registration: |
N107KW |
Aircraft: |
Bowers FLYBABY |
Injuries: |
1 Fatal |
Flight Conducted Under: |
Part 91: General Aviation - Personal |
On October 19, 2018, at 1130 central daylight time, an experimental, amateur-built Bowers Flybaby, N107KW, was substantially damaged after impacting trees and terrain near Milton, Florida. The airline transport pilot was fatally injured. Visual meteorological conditions prevailed, and no flight plan was filed for the flight that was conducted under the provisions of Title 14 Code of Federal Regulations Part 91. The flight departed George T. McCutchan Airport (8FL6), Harold, Florida, around 1100.
The owner/operator of the airplane reported that pilot was his friend and a highly experienced military and airline pilot. The pilot routinely flew the airplane to either Yellow River Airstrip (FD93), Holt, Florida, or Baker Sky Ranch, a private airport, but the owner was unsure where the pilot was flying to on the day of the accident. He also stated that there were no known issues with the airplane.
Several witnesses observed the flight and stated that the airplane was flying west-southwest and paralleling the highway 500 ft above ground level (agl) about 2 miles northwest of FD93. They stated that the airplane's engine sounded like it was modulating back and forth from normal power to no power on a regular interval. One witness said the engine sounded smooth when it had power, however, it then went quiet for about 10 seconds before starting back up again; "it did this several times." The airplane descended to about 100 ft agl, just above the tree tops when the wings started to rock back and forth. The airplane then made a left turn to the south, immediately rolled left and descended steeply until impact. Another witness stated he heard a "backfire" as the airplane was descending.
The airplane collided with trees and terrain on a heading of about 120° in a heavily wooded area next to a farm. The wreckage path was compact; all primary structural components and flight control surfaces were accounted for in the debris field. There were several broken branches about 20 ft agl in nearby trees and the airplane struck the ground in a nose down angle. The propeller remained attached to the flange and one blade was broken backwards but remained attached to the hub. The engine remained attached to the firewall, which was separated from the fuselage. The left wing separated from the fuselage and was broken in several locations. The airplane had numerous breaks and tears in the fuselage. The tail section, including the rudder and elevators remained attached and showed little sign of damage. The 12-gallon fuel tank mounted on the firewall was compromised during the accident sequence and contained about 2 gallons of 100 low lead aviation gasoline. There was no post-accident fire.
The wreckage was retained for further examination.
NTSB Identification: NYC69D0223
Incident occurred Sunday, October 13, 1968 at CORAM, NY
Aircraft:FLY BABY 1A, registration: N343Y
Injuries: Unavailable
TYPE OF ACCIDENT
GROUND-WATER LOOP-SWERVE - LANDING: ROLL
COLLIDED WITH: PARKED AIRCRAFT - LANDING:
ROLL
PROBABLE CAUSE(S)
PILOT IN COMMAND - IMPROPER OPERATION OF BRAKES
AND/OR FLIGHT CONTROLS FACTOR(S)
PILOT IN COMMAND - LACK OF FAMILIARITY WITH
AIRCRAFT
REMARKS- FIRST FLT IN ACFT. PLTS FOOT SLIPPED
OFF
BRAKE PEDAL, HIT N4615M, SUBS DAMAGE.
NTSB Identification: NYC71FNE34
Incident occurred Thursday, May 20, 1971 at OXFORD, CT
Aircraft:FLYBABY 1A, registration: N3314
Injuries: Unavailable
TYPE OF ACCIDENT
AIRFRAME FAILURE: IN FLIGHT
PROBABLE CAUSE(S)
AIRFRAME - WINGS: WING ATTACHMENT FITTINGS,BOLTSFACTOR(S)
MISCELLANEOUS ACTS,CONDITIONS - FATIGUE FRACTURE
MISCELLANEOUS ACTS,CONDITIONS - CORRODED/CORROSION
PERSONNEL - MAINTENANCE,SERVICING,INSPECTION: INADEQUATE INSPECTION OF AIRCRAFT (OWNER-PILOT)
REMARKS- L WG FLYING WIRE TURNBUCKLE FAILED. WG SEPARATED. PLT PARACHUTED SUCCESSFULLY.
NTSB Identification: FTW71FPM29
Incident occurred Monday, May 31, 1971 at DURANT, OK
Aircraft:FLY BABY 1-14, registration: N7347
Injuries: Unavailable
TYPE OF ACCIDENT
AIRFRAME
FAILURE: IN FLIGHT
PROBABLE CAUSE(S)
AIRFRAME - WINGS: BRACING WIRES,STRUTSFACTOR(S)
AIRFRAME - WINGS: OTHER
MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD FAILURE
MISCELLANEOUS ACTS,CONDITIONS - PREVIOUS DAMAGE
REMARKS- 3 FLYING WIRES,R WING,PULLED THRU NICOPRESS,GR AXLE ATCH PNT,4TH,WING ATCH.GR AXLE PREV DMG.
[RJW Note: The report on this one listed the pilot as having one hour of Fly Baby time. From the comment about "previous damage" I suspect the aircraft had been damaged on that first flight and not properly repaired.]
NTSB Identification: MIA72FKG60
Incident occurred Saturday, December 11, 1971 at WINDER, GA
Aircraft:FLY BABY SWORDS, registration: N2011
Injuries: Unavailable
TYPE OF ACCIDENT
AIRFRAME FAILURE: IN FLIGHT -- IN FLIGHT
ACROBATICS
PROBABLE CAUSE(S)
AIRFRAME - WINGS: BRACING WIRES,STRUTSREMARKS- L WG AND SUPPORT WIRES FAILED.CABLE EYES SPLICED IMPROPERLY.PLT WAS ADVISED NOT TO FLY ACROBATICS.
MISCELLANEOUS ACTS,CONDITIONS - IMPROPERLY INSTALLED
PERSONNEL - PRODUCTION-DESIGN-PERSONNEL: OTHER
PILOT IN COMMAND - EXCEEDED DESIGNED STRESS LIMITS OF AIRCRAFT
MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD FAILURE
NTSB Identification: SEA73FYE08
Incident occurred Wednesday, July 26, 1972 at KELSO, WA
Aircraft:FLYBABY M-1, registration: N8716
Injuries: Unavailable
TYPE OF ACCIDENT
COLLISION WITH AIRCRAFT: BOTH ON GROUND -
LANDING: ROLL
PROBABLE CAUSE(S)
PILOT
IN COMMAND - FAILED TO SEE AND AVOID OTHER AIRCRAFT
FACTOR(S)
PILOT IN COMMAND - PHYSICAL IMPAIRMENT
PILOT IN COMMAND - ATTEMPTED OPERATION W/KNOWN
DEFICIENCIES
IN EQUIPMENT
REMARKS- N8716 NOT EQUIPPED WITH NAV LTS.PLT OF N8716 WAS
MEDICALLY
RESTRICTED FROM NITE FLT.UNCONTRLDARPT
NTSB Identification: MKC73DCD16
Incident occurred Saturday, August 12, 1972 at OSAGE, IA
Aircraft:BOWERS FLY BABY, registration: N48ML
Injuries: Unavailable
TYPE OF ACCIDENT
COLLIDED WITH:
FENCE,FENCEPOSTS
LANDING:
FINAL
APPROACH
PROBABLE CAUSE(S)
PILOT IN COMMAND - SELECTED UNSUITABLE TERRAIN
PILOT IN COMMAND - MISJUDGED ALTITUDE
FACTOR(S)
AIRPORTS/AIRWAYS/FACILITIES
- AIRPORT CONDITIONS: OTHER
NTSB Identification: NYC73DKM24
Incident occurred Friday, January 19, 1973 at HENDERSONVILLE, NC
Aircraft:FLYBABY M-1, registration: N808RJ
Injuries: Unavailable
TYPE OF ACCIDENT
ENGINE FAILURE OR MALFUNCTION -- TAKEOFF:
INITIAL
CLIMB
GEAR COLLAPSED-- LANDING: LEVEL OFF/TOUCHDOWN
PROBABLE CAUSE(S)
PILOT IN COMMAND - IMPROPER OPERATION OF
POWERPLANT
& POWERPLANT CONTROLS
MISCELLANEOUS ACTS,CONDITIONS - ICE-CARBURETOR
PILOT IN COMMAND - IMPROPER LEVEL OFF
FACTOR(S)
PILOT IN COMMAND - INADEQUATE PREFLIGHT
PREPARATION
AND/OR PLANNING
WEATHER - CONDITIONS CONDUCIVE TO
CARB./INDUCTION
SYSTEM ICING
MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD
FAILURE
PARTIAL POWER LOSS - PARTIAL LOSS OF POWER - 1
ENGINE
EMERGENCY CIRCUMSTANCES - FORCED LANDING OFF
AIRPORT
ON LAND
NTSB Identification: IAD73ILQ26
Incident occurred Tuesday, April 17, 1973 at GREENVILLE, KY
Aircraft:FLY BABY 1-A, registration: N2207
Injuries: Unavailable
TYPE OF ACCIDENT
STALL --- TAKEOFF: INITIAL CLIMB
PROBABLE CAUSE(S)
PILOT IN COMMAND - FAILED TO OBTAIN/MAINTAIN
FLYING
SPEED
FACTOR(S)
WEATHER - DOWNDRAFT,UPDRAFTS
NTSB Identification: SEA74DYI03
Incident occurred Saturday, July 21, 1973 at BANDON, OR
Aircraft:FLYBABY , registration: N1432
Injuries: Unavailable
TYPE OF ACCIDENT
ENGINE FAILURE OR MALFUNCTION --- IN FLIGHT:
DESCENDING
COLLIDED WITH: TREES --- LANDING: FINAL
APPROACH
PROBABLE CAUSE(S)
PILOT IN COMMAND - ATTEMPTED OPERATION W/KNOWN
DEFICIENCIES
IN EQUIPMENT
WEATHER - CONDITIONS CONDUCIVE TO
CARB./INDUCTION
SYSTEM ICING
MISCELLANEOUS ACTS,CONDITIONS - ICE-CARBURETOR
PARTIAL POWER LOSS - PARTIAL LOSS OF POWER - 1
ENGINE
EMERGENCY CIRCUMSTANCES - FORCED LANDING OFF AIRPORT ON LAND
REMARKS- EXP TEST FLT.INADQT CARB HEATER MUFFS.LNDD IN TREE.
NTSB Identification: LAX74FUJ20
Incident occurred Saturday, September 22, 1973 at ASHFORK, AZ
Aircraft:BOWERS FLY BABY, registration: N247AF
Injuries: Unavailable
TYPE OF ACCIDENT
ENGINE FAILURE OR MALFUNCTION -- TAKEOFF:
INITIAL
CLIMB
COLLIDED WITH: TREES -- LANDING: ROLL
PROBABLE CAUSE(S)
POWERPLANT - FUEL SYSTEM: CARBURETOR
MISCELLANEOUS ACTS,CONDITIONS -
LOOSE,PART/FITTING
MISCELLANEOUS ACTS,CONDITIONS - FUEL STARVATION
PARTIAL POWER LOSS - PARTIAL LOSS OF POWER - 1
ENGINE
EMERGENCY CIRCUMSTANCES - FORCED LANDING OFF
AIRPORT
ON LAND
REMARKS- CARB FLOAT NEEDLE SEAT LOOSE.ACFT BUILT & OPERATED
BY
PUBLIC
SCHOOL.SECOND FLT.
NTSB Identification: NYC74FNC28
Incident occurred Sunday, October 28, 1973 at SOUTH PARIS, ME
Aircraft:BOWERS FLY BABY, registration: NONE
Injuries: Unavailable
TYPE OF ACCIDENT
STALL --- IN FLIGHT: BUZZING
PROBABLE CAUSE(S)
PILOT IN COMMAND - FAILED TO OBTAIN/MAINTAIN
FLYING
SPEED
PILOT IN COMMAND - LACK OF FAMILIARITY WITH
AIRCRAFT
FACTOR(S)
MISCELLANEOUS
ACTS,CONDITIONS - STOLEN OR UNAUTH=
REMARKS- COMPLETED LOW PASS PULLED ACFT STRAIGHT UP MADE TURN TO
R.ACFT
NOT REGISTERED.
[RJW note: Hmmm..."Stolen or unauthorized"..."Aircraft not
registered..."
Sounds like there's an interesting story behind this one...]
NTSB Identification: SEA74FTA18
Incident occurred Saturday, March 09, 1974 at COLSTRIP, MT
Aircraft:FLY BABY HUEY, registration: N1062H
Injuries: Unavailable
TYPE OF ACCIDENT
STALL -- LANDING: TRAFFIC PATTERN-CIRCLING
PROBABLE CAUSE(S)
PILOT IN COMMAND - FAILED TO OBTAIN/MAINTAIN
FLYING
SPEED
PILOT IN COMMAND - IMPROPER OPERATION OF FLIGHT
CONTROLS
REMARKS- STALLED AT LOW ALTITUDE.
NTSB Identification: SEA74FYC56
Incident occurred Monday, May 27, 1974 at SALEM, OR
Aircraft:MAY FLYBABY 1, registration: N93003
Injuries: Unavailable
TYPE OF ACCIDENT
AIRFRAME FAILURE: IN FLIGHT -- ACROBATICS
PROBABLE CAUSE(S)
PILOT IN COMMAND - EXCEEDED DESIGNED STRESS
LIMITS
OF AIRCRAFT
PILOT IN COMMAND - FAILED TO FOLLOW APPROVED
PROCEDURES,DIRECTIVES,ETC.
FACTOR(S)
AIRFRAME - WINGS: SPARS
MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD
FAILURE
MISCELLANEOUS ACTS,CONDITIONS - SEPARATION IN
FLIGHT
REMARKS- RIGHT WING SEPARATED DURING PROHIBITED LOOP MANEUVERS.
NTSB Identification: SEA75FYC05
Incident occurred Saturday, July 20, 1974 at HUBBARD, OR
Aircraft:FLY BABY 1, registration: N4604
Injuries: Unavailable
TYPE OF ACCIDENT
UNDERSHOOT -- LANDING: FINAL APPROACH
COLLIDED WITH: CROP --- LANDING: LEVEL
OFF/TOUCHDOWN
PROBABLE CAUSE(S)
PILOT IN COMMAND - MISJUDGED DISTANCE AND
ALTITUDE
FACTOR(S)
TERRAIN - HIGH VEGETATION
REMARKS- LND IN TALL WHEAT.
NTSB Identification: CHI75FEE06
Incident occurred Saturday, July 27, 1974 at LOCKPORT, IL
Aircraft:BOWERS FLY BABY, registration: N337X
Injuries: Unavailable
TYPE OF ACCIDENT
COLLISION WITH AIRCRAFT: BOTH ON LANDING:
ROLL
PROBABLE CAUSE(S)
PERSONNEL - MISCELLANEOUS-PERSONNEL: PILOT OF
OTHER
AIRCRAFT
FACTOR(S)
MISCELLANEOUS - EVASIVE MANEUVER TO AVOID
COLLISION
MISCELLANEOUS ACTS,CONDITIONS - INTENTIONAL
GROUND-WATER-LOOP-SWERVE
REMARKS- CESSNA N18534 ENTRD AND STARTED TO CROSS RWY IN FRONT OF N337X ON LDG ROLL.
NTSB Identification: OAK76FVM05
Incident occurred Friday, August 08, 1975 at FREMONT, CA
Aircraft:FLYBABY 1A, registration: N41837
Injuries: Unavailable
TYPE OF ACCIDENT
COLLISION WITH GROUND/WATER: UNCONTROLLED --
LANDING:
TRAFFIC PATTERN-CIRCLING
PROBABLE CAUSE(S)
PILOT IN COMMAND - ATTEMPTED OPERATION W/KNOWN
DEFICIENCIES
IN EQUIPMENT
MISCELLANEOUS ACTS,CONDITIONS - PREVIOUS DAMAGE
FACTOR(S)
PILOT IN COMMAND - LACK OF FAMILIARITY WITH
AIRCRAFT
REMARKS- LDG FROM PRIOR 15MIN FLT BENT RT AXLE AND LOOSENED RT WING FLYING WIRES.
NTSB Identification: LAX76AL017
Incident occurred Thursday, September 04, 1975 at CORONA, CA
Aircraft:FLY BABY 1A, registration: N4356
Injuries: Unavailable
TYPE OF ACCIDENT
COLLISION WITH AIRCRAFT: BOTH IN FLIGHT
--
LANDING: FINAL APPROACH
PROBABLE CAUSE(S)
PERSONNEL - MISCELLANEOUS-PERSONNEL: PILOT OF
OTHER
AIRCRAFT
FACTOR(S)
PILOT IN COMMAND - FAILED TO SEE AND AVOID
OTHER
AIRCRAFT
REMARKS- C-150 DIDNT CALL UNICOM. FLYBABY NOT RADIO EQUIPPED.
NTSB Identification: MIA76FKT81
Incident occurred Saturday, June 05, 1976 at FT LAUDERDALE, FL
Aircraft:FLY BABY 1A, registration: N3776
Injuries: Unavailable
TYPE OF ACCIDENT
AIRFRAME FAILURE: IN FLIGHT -- IN
FLIGHT:
NORMAL CRUISE
PROBABLE CAUSE(S)
PERSONNEL - MAINTENANCE,SERVICING,INSPECTION:
INADEQUATE
MAINTENANCE AND INSPECTION
AIRFRAME - WINGS: SPARS
MISCELLANEOUS ACTS,CONDITIONS - MATERIAL
FAILURE
MISCELLANEOUS ACTS,CONDITIONS - DETERIORATED
FACTOR(S)
MISCELLANEOUS ACTS,CONDITIONS - SEPARATION IN
FLIGHT
PILOT IN COMMAND - EXERCISED POOR JUDGMENT
REMARKS- R WG SEPARATED. LAST ANNUAL INSPECTION-JULY 1971.
NTSB Identification: NYC76FGT76
Incident occurred Wednesday, August 25, 1976 at KRALLTOWN, PA
Aircraft:BOWERS FLY BABY, registration: N8Q
Injuries: Unavailable
TYPE OF ACCIDENT
STALL: SPIN -- TAKEOFF: INITIAL CLIMB
PROBABLE CAUSE(S)
PILOT IN COMMAND - FAILED TO OBTAIN/MAINTAIN
FLYING
SPEED
FACTOR(S)
PILOT IN COMMAND - LACK OF FAMILIARITY WITH
AIRCRAFT
REMARKS- DURING FAMIL FLT IN NEW TYPE AFCT PLT ALLOWED AFCT TO
STALL
DURING CLIMB AFTER TAKEOFF.
NTSB Identification: CHI77FEC35
Incident occurred Friday, June 17, 1977 at FLINT, MI
Aircraft:FLY BABY 1-A, registration: N7105
Injuries: Unavailable
TYPE OF ACCIDENT
ENGINE FAILURE OR MALFUNCTION -- TAKEOFF:
INITIAL
CLIMB
NOSE OVER/DOWN -- LANDING: ROLL
PROBABLE CAUSE(S)
PERSONNEL - MAINTENANCE,SERVICING,INSPECTION:
INADEQUATE
MAINTENANCE AND INSPECTION
POWERPLANT - ENGINE STRUCTURE: PISTON,PISTON
RINGS
POWERPLANT - ENGINE STRUCTURE: VALVE ASSEMBLIES
MISCELLANEOUS ACTS,CONDITIONS - LOW COMPRESSION
PARTIAL POWER LOSS - PARTIAL LOSS OF POWER - 1
ENGINE
EMERGENCY CIRCUMSTANCES - FORCED LANDING OFF AIRPORT ON LAND
REMARKS- #4CYL EXH VALVE STREAKED,NOT CLOSING PROPERLY.ALL PISTON RING GAPS EXCESS OF MAX ALLOWABLE.
NTSB Identification: FTW78DRG56
Incident occurred Sunday, June 25, 1978 at SAN ANTONIO, TX
Aircraft:FLYBABY FB-1A, registration: N1584
Injuries: Unavailable
TYPE OF ACCIDENT
GROUND-WATER LOOP-SWERVE -- LANDING:
LEVEL
OFF/TOUCHDOWN
NOSE OVER/DOWN -- LANDING: ROLL
PROBABLE CAUSE(S)
PILOT IN COMMAND - IMPROPER LEVEL OFF
PILOT IN COMMAND - IMPROPER RECOVERY FROM
BOUNCED
LANDING
FACTOR(S)
WEATHER - UNFAVORABLE WIND CONDITIONS
TERRAIN - HIGH VEGETATION
REMARKS- ACFT BOUNCED AT TOUCHDOWN,VEERED INTO TALL GRASS ALONG
RUNWAY.
NTSB Identification: NYC79FFJ06
Incident occurred Sunday, October 01, 1978 at JAVA CENTER, NY
Aircraft:FLY BABY JD-1, registration: N12JD
Injuries: Unavailable
TYPE OF ACCIDENT
COLLISION WITH GROUND/WATER: CONTROLLED
--
LANDING: TRAFFIC PATTERN-CIRCLING
PROBABLE CAUSE(S)
MISCELLANEOUS - UNDETERMINED
REMARKS- ACFT OBSVD TO ROLL ON DOWNWIND LEG OF TRAFFIC PATTERN.SEAT BELT FAILED AT ANCHOR POINT.
NTSB Identification: MIA79FLG06
Incident occurred Saturday, December 02, 1978 at MONCKS CORNER,
SC
Aircraft:FLY BABY 1A, registration: N8371
Injuries: Unavailable
TYPE OF ACCIDENT
AIRFRAME FAILURE: IN FLIGHT --:
ACROBATICS
PROBABLE CAUSE(S)
PILOT IN COMMAND - EXCEEDED DESIGNED STRESS
LIMITS
OF AIRCRAFT
FACTOR(S)
AIRFRAME - WINGS: SPARS
MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD
FAILURE
MISCELLANEOUS ACTS,CONDITIONS - SEPARATION IN
FLIGHT
REMARKS- L WING SEPARATED.
NTSB Identification: SEA79DYP26
Incident occurred Sunday, June 03, 1979 at SPANGLE, WA
Aircraft:FLYBABY 1, registration: N2283Z
Injuries: Unavailable
TYPE OF ACCIDENT
ENGINE FAILURE OR MALFUNCTION -- LANDING:
TRAFFIC
PATTERN-CIRCLING
HARD LANDING -- LANDING: LEVEL
OFF/TOUCHDOWN
PROBABLE CAUSE(S)
PERSONNEL - MAINTENANCE,SERVICING,INSPECTION:
INADEQUATE
MAINTENANCE AND INSPECTION
POWERPLANT - FUEL SYSTEM: CARBURETOR
MISCELLANEOUS ACTS,CONDITIONS - IMPROPERLY
SECURED
MISCELLANEOUS ACTS,CONDITIONS - FUEL STARVATION
PILOT IN COMMAND - IMPROPER LEVEL OFF
FACTOR(S)
MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD
FAILURE
COMPLETE POWER LOSS - COMPLETE ENGINE
FAILURE/FLAMEOUT-1
ENGINE
EMERGENCY CIRCUMSTANCES - FORCED LANDING ON
AIRPORT/SEAPLANE
BASE/HELIPT.
REMARKS- CARB NEEDLE VALVE SEAT NOT SAFETIED,BACKED OUT.
AIRFRAME FAILURE: IN FLIGHT IN FLIGHT: ACROBATICS
PROBABLE CAUSE(S)
PILOT IN COMMAND - EXCEEDED DESIGNED STRESS LIMITS OF AIRCRAFT
FACTOR(S)
PILOT IN COMMAND - PHYSICAL IMPAIRMENT
MISCELLANEOUS ACTS,CONDITIONS - ALCOHOLIC IMPAIRMENT OF EFFICIENCY AND JUDGMENT
AIRFRAME - WINGS: SPARS
MISCELLANEOUS ACTS,CONDITIONS - OVERLOAD FAILURE
MISCELLANEOUS ACTS,CONDITIONS - SEPARATION IN FLIGHT
REMARKS- PLT BLOOD ALCOHOL LEVEL .06%.
NTSB Identification: NYC79FHJ28
Incident occurred Wednesday, August 08, 1979 at SHIRLEY, NY
Aircraft:FLYBABY 1B, registration: N78FP
Injuries: Unavailable
TYPE OF ACCIDENT
HARD LANDING -- LANDING: LEVEL
OFF/TOUCHDOWN
GEAR COLLAPSED -- LANDING: LEVEL
OFF/TOUCHDOWN
PROBABLE CAUSE(S)
PILOT IN COMMAND - IMPROPER LEVEL OFF
NTSB Identification: MKC80FER37
Incident occurred Saturday, April 26, 1980 at WAUBUN, MN
Aircraft:FLY BABY BWM-10, registration: N1081Z
Injuries: Unavailable
TYPE OF ACCIDENT
AIRFRAME FAILURE: IN FLIGHT -- ACROBATICS
PROBABLE CAUSE(S)
PERSONNEL - MAINTENANCE,SERVICING,INSPECTION:
INADEQUATE
MAINTENANCE AND INSPECTION
PILOT IN COMMAND - IMPROPER IN-FLIGHT DECISIONS
OR PLANNING
AIRFRAME - WINGS: WING ATTACHMENT
FITTINGS,BOLTS
MISCELLANEOUS ACTS,CONDITIONS - IMPROPERLY
INSTALLED
MISCELLANEOUS ACTS,CONDITIONS - MATERIAL
FAILURE
REMARKS- L WG REAR ATCH BOLT PULLED LOOSE.HOLE IMPROPERLY DRILLED,BUSHING NOT INSTLD.ACFT RSTRD FM ACRO FLT
NTSB Identification: CHI81FEK16
Incident occurred Thursday, April 30, 1981 at ZANESVILLE, OH
Aircraft:FLY BABY 1A, registration: N609X
Injuries: Unavailable
TYPE OF ACCIDENT
STALL: SPIN -- TAKEOFF: INITIAL
CLIMB
PROBABLE CAUSE(S)
PILOT IN COMMAND - FAILED TO OBTAIN/MAINTAIN
FLYING
SPEED
NTSB Identification: MKC81FCG53
Incident occurred Friday, August 14, 1981 at PAOLA, KS
Aircraft:FLYBABY 1A-BIS, registration: N59229
Injuries: Unavailable
TYPE OF ACCIDENT
STALL -- LANDING: FINAL APPROACH
PROBABLE CAUSE(S)
PILOT IN COMMAND - FAILED TO OBTAIN/MAINTAIN
FLYING
SPEED
FACTOR(S)
PILOT IN COMMAND - LACK OF FAMILIARITY WITH
AIRCRAFT
INSTRUMENTS/EQUIPMENT AND ACCESSORIES - FLIGHT
AND
NAVIGATION INSTRUMENTS: AIRSPEED
MISCELLANEOUS ACTS,CONDITIONS - ERRATIC
REMARKS- 1ST FLT IN THIS MAKE & MODEL.PLT RPRTD PSBL AIRSPEED
MALFUNCTION.EQUIPPED
W 65HP LYCOMING ENG.
NTSB Identification: DEN83FTM01
Accident occurred Saturday, October 16, 1982 at EPHRIAM, UT
Aircraft:BOWERS FLY BABY 1A, registration: N63498
Injuries: 1 Fatal.
APPROXIMATELY 4 FT OF THE INBOARD SECTION OF THE LEFT WING SEPARATED IN FLIGHT DURING AN AEROBATIC MANEUVER. WITNESSES STATED THAT THE ACFT HAD BEEN PERFORMING LITTLE LOOPS & THEN IT WENT STRAIGHT UP & ROLLED OFF TO THE LEFT UPSIDE DOWN. IT THEN SPIRALLED ONCE OR TWICE, STRAIGHTENED OUT, MADE A SLIGHT RIGHT TURN & THEN THE WING FAILED. THE LATEST OPERATING LIMITATIONS FOR THE AMATEUR BUILT ACFT SPECIFICALLY PROHIBITS ANY INTENTIONAL AEROBATIC FLT MANEUVERS.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows.
PROCEDURES/DIRECTIVES..DISREGARDED..PILOT IN COMMANDContributing Factors
AEROBATICS..PERFORMED..PILOT IN COMMAND
DESIGN STRESS LIMITS OF AIRCRAFT..EXCEEDED..PILOT IN COMMAND
WING..OVERLOAD
WING..FAILURE,PARTIAL
WING..SEPARATION